ACTIVITY REPORT OFFICE OF SPECIAL ACTIVITIES NOVEMBER 1966

Document Type: 
Collection: 
Document Number (FOIA) /ESDN (CREST): 
CIA-RDP68B00724R000100100006-4
Release Decision: 
RIPPUB
Original Classification: 
T
Document Page Count: 
6
Document Creation Date: 
December 12, 2016
Document Release Date: 
June 3, 2002
Sequence Number: 
6
Case Number: 
Publication Date: 
December 11, 1966
Content Type: 
REPORT
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PDF icon CIA-RDP68B00724R000100100006-4.pdf224.46 KB
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Approved,For ReI 24R000100100006-4 2906-66 Copy-to-of 1 0 1 1 DEC 1966 ACTIVITY REPORT OFFICE OF SPECIAL ACT: TrIES NOVEMBER 1966 25X1 I , C:OART A. DEVELOPMENT SUMMARY AND PROC 3S 1. AIRFRAME No change. 2. PROPULSION a. A flight test pro--yam was initiated on Aircraft rr127 to evaluate various designs of Main Engine Fuel Control TT2 (compressor inlet temperature) Sensors as a result of recent failures, see October OSA Activities report Test sensors were strain raged in an e or to e ermine if any particular con- dition of flight produces stresses which might affect their structural integrity. Flight data includes EGT (exhaust gas temperature), engine RPM and TT2 in order to determine the response rate and accuracy of EGT and RPM scheduling of main fuel controls in combination with various TT2 sensors. The flight test program is nearly complete with the preliminary analysis of the data gathered to date indicating the presently specified sensor design (center strut supported, three loop coil) provides the best combination of response rate and structural inte rit . Ten units of this design have been received with further deliveries presently programm e of three to four units per week. b. Detachment aircraft were grounded, as a precautionary measure, for approximately ten days in November due to an undefined contaminant being dis- covered in the fuel tanks of several aircraft. The contaminant was later attributed to be a chemical derivative of improperly cured fuel tank sealant material. Laboratory tests determined the contaminant as insoluble in fuel over the temperature range the fuel encounters in operations. As a result, the foreign particles, when they occur in the tank, will be screened out by the aircraft 25X1 and engine fuel filtering system. 25X1 Approved For Rele TOP SECRET Approved For Releao e 2002/08T120 - OP CA- 8BOM4ROO01001 2906-66 25X1 age 2 c. Several range extension test flights were conducted on flight test aircraft #121. The major propulsion system modification incorporated on these flights involves an improved seal system for the "basket" assembly which constitutes the forward bypass bleed door system. Carefully fitted U-shaped stainless steel seals are being utilized in lieu of the standard Viton seals in this area. Prelf.-_i},...'y : ,ults of these tests indicate that inlet lc;.... t .::~ i fL -,,;duced from 8% to 3% of the air entering the inlet. The early results indicate an inlet recovery of approximately 76.5% which was reduced somewhat due to the inlet -forward bypass doors being open an average of .3 inches. A planned revision of the forward door position/pressure schedule, to assure that the forward doors are closed at Cruise Mach numbers, with the improved seals, could potentially raise the inlet recovery to approximate the design matched inlet recovery value of 80%. 25X1 3. PAYLOAD c. Seven (7) photo configuration sorties were flown with the following results. Type No. of Flights i Two (2 ) Ii Two (2) IV Three (3) Satisfactory Satisfactory (1) Satisfactory (2) Unsatisfactory* *One shutdown after nine (9) minutes operation caused by malfunctioning V/H sensor which caused film to wrap around metering and transport roller. One malfunction after ten (10) minutes of operation caused by defective 400 cycle relay feeding the V/H sensor. 25X1 Approved For Release 2002/08/2&PCl i B00724R004 Approved For Release 2002/08/20 : CIA-RDP68B.00724R000100100006-4 TOP ,`irx;ltP;'1. 119Ot; 25X1 Flights Time Total Total Aircraft November November Flights Hours 121 5 6:51 254 273:04 122 - - 157 169:39 123 - - 78 136:10 124 17 30:40 531 937:50 125 4 6:55 198 320:10 126 - - 104 169:16 127 3 4:45 179 305:10 128 4 9:35 162 299:30 1.29 4 10:40 186 240:29 130 2 2:25 1%16 252:1:') L31. Al- 9: 45 96 157 : 05 132 1 1:15 126 208:57 133 - - 9 8:17 B. OPERATIONAL SUMMARY AND PROGRESS 1. EMERGENCY CAPABILITY (SKYLARK): No change. 2. CONTINGENCY PLANNING - FAR EAST (PINWHEEL): No change. 4. FORWARD BASE EXERCISE: 25X1 A Forward Base Exercise was conducted from Kadena Air Base, Okinawa, during the week of 14 November 1966. Purpose of this FBX was to exercise all procedures required to fly a PINWHEEL operational mission. Notification procedures Vhrough JCS/JRC to CINCPAC, radar suppression and air space blocking in all areas of operation and weather scout procedures were exercised and found to be adequate. In addition, Detachment, host base and supporting commands were exercised. Overall the FEX was highly successful and there were no problem areas that would preclude flying operational PINWHEEL missions this date. . 25X1 Approved For Release 2002/08/20 : CIA-RDP68B00724R00J0100100006-4 Approved For Release 2002/08/20 : CIA-RDP68B00724R000100100006-4 TOP SECRET 2906-66 Page 4 5. PROJECT PILOT INVENTORY: a. ready. Project Pilots are currently operationally b. newly assigned Project Pilots in training for operationally ready status. 6. A-12 AIRCRAFT: No change. 7. PERFORMANCE STATISTICS: a. All performance statistics as reported in )ctober 1966 report remain unchanged with the following exceptions: 1. Average A-12 Time-Operationally Ready Detachment Pilots ............................ 2. Assigned Detachment Pilots ........... 25X1 25X1 25X1 II, IDEALIST A. DEVELOPMENT SUMMARY AND PROGRESS 1. A U-2R Cockpit Mock-up Review meeting was held at Lockheed Aircraft, Burbank, California, on 29 and 30 November. In addition to a detailed cockpit critique by pilots in full pressure suits, the model specifications, spares support and ,he baseline configuration with respect to 25X1 Corn-Nav equipment were reviewed. At this time, no specific problem areas could be identified and the program is proceeding on schedule. B. OPERATIONAL SUMMARY AND PROGRESS Approved For Release 200F8 /2SQ ffi-?ZDP68B0072 R000100100006-4 25X1 25X1 e 2002/08/20 : CIA-RDP68BGW24R000100100006-4 TOP SECRET I 2906-66 25X1 Page 5 25X1 e. Two successful flight tests were flown during the month for checking out the modified "H" configuration in preparation for the shipment of this unit. 25X1 f. One flight test was flown for the purpose of obtaining fuel data with a 1720 gallon load. Excellent fuel consumption information was obtained and the test was classified as successful. 2. PRODUCT IMPROVEMENT a. Four APN-153/ASN-66 Doppler Navigation Systems have been contracted for with the first system delivery scheduled for January 1967. b. No tests were flown on the Air Data Computer/ Tape Altimeter due to the higher priority of other requirements. Tests should be completed during the month of December. No change. 25X1 Approved For Release 2002/0b ~k68B00724R 00100100006-4 002/08/20 : CIA-RDP68B0070001001000 E I TOP SECRET 2906_66 25X1 age 6 MARD/COMP`2/OS A ~ Distribution: (11 Dec 66) Cy 1, 2, 3, 4 - C/P&PS/DD/S&T 5 - D/SA 6 - D/O/OSA 7 - D/R&D/OSA 8,9 - BPD/OSA 10 - RB/OSA 25X1 Approved For Release 2002/08/20 : CIA-RDP68B00724R000100100006-4