ACTIVITY REPORT OFFICE OF SPECIAL ACTIVITIES OCTOBER 1966

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Collection: 
Document Number (FOIA) /ESDN (CREST): 
CIA-RDP68B00724R000100090031-8
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RIPPUB
Original Classification: 
T
Document Page Count: 
8
Document Creation Date: 
December 14, 2016
Document Release Date: 
July 29, 2003
Sequence Number: 
31
Case Number: 
Publication Date: 
November 10, 1966
Content Type: 
REPORT
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PDF icon CIA-RDP68B00724R000100090031-8.pdf333.34 KB
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Approved For Release 2003/0/$ :0JP68B007.24R000100090031-8 25X1A OXCART/IDEALIST, ACTIVITY REPORT OFFICE OF SPECIAL ACTIVITIES OCTOBER 1966 I. OXCART A. DEVELOPMENT SUMMARY AND PROGRESS 1. AIRFRAME 10 NOV 1966 a, Aircraft 127 made its first flight on 11 October after service bulletin modifications were completed. On 18 October, aircraft 127 flew a seven hour, forty minute mission which represents the longest A-12 flight to date. On 12 October, aircraft 129 had flown a seven hour, thirty-five minute flight which was the previous record. b. A meeting was held at Project Headquarters of the Headquarters' members of the OXCART Aircraft Configuration and Flight Test Control Board. The purpose of this meeting was to review completed staff actions resulting from the CCB meeting held on 22 September 25X1A 25X1A 25X1 2. PROPULSION a. Fuel conforming to the revised (523-E) fuel specification is presently being received 25X1A The new fuel should eliminate the contamination pro em that has affected certain engine fuel system components. By flushing aircraft fuel systems and through a program of monitoring fuel system components, already installed, just delivered from overhaul verification; it will be established that the fuel contaminant accumulation problem has been eliminated. b. On 25 October, following the sixth failure of a Hamilton Standard, Engine Main Fuel Control TT2 Sensor (compressor inlet temperature), all articles were grounded until the problem could be resolved. As an interim solution, the sensors of the design, which have been failing will be replaced by an earlier design which are currently used as the Afterburner Fuel Control TT2 Sensors, CROUP t Exxicc :; tram autamatlc t`ss^ ra~lr~ and OXCART/IDEALIST/ Copy Oof /('j TOP SECRET' lease 2003/08/18 : CIA-RDP68B00724R - 25X1A 25X1A TOP SECRET Approved For Release 2003/08/18 : CIA-RDP68B00724R000100090031-8 25X1A Page 2 The older sensors have a more rugged design than-the later models but have a slower response rate. It is expected that the Afterburner Fuel Control TT2 Sensor will provide adequate main fuel control with the possible exception that the pilot will have to perform more hand trimming of the exhaust gas temperature. At present fourteen spare afterburner control type sensors are available and are being installed on engines. If necessary more sensors can be obtained by borrowing from inactive afterburner controls. c. Procurement has been initiated for two new ?TT2 Sensor designs for the main fuel control from Hamilton Standard. Sensors reflecting these changes will start being received on or about 23 November 1966. In addition, there are a total of nine YJ engines equipped with Bendix main fuel controls which utilize a different style TT2 sensor. Seven of these engines are now being brought up to BLACKSHIELD configuration on an expedited basis. 3. PAYLOAD c. Eleven (11) photo configuration sorties were flown during October with the following results. Type No. of Flights I Six (6) II Two (2) IV Two (2) One (1) TOP SECRET Approved For Release 2003/08/18: CIA-RDP68B00724R Satisfactory Satisfactory .Satisfactory Failure - After twenty- two minutes operation, one shuffle roller malfunctioned and jammed into the film. Simple modification will prevent reoccurrencF 25X1A 25X1 A- Approved For Releas Page 3 4. AIRCRAFT FLIGHT TEST SUMMARY 25X1A Aircraft Flights October Time October Total Flights Total Hours 121 3 7:10 249 266:13 122 - - 157 169:39 123 - - 78 136:10 124 14 25:00 514 907:10 125 5 9:15 194 313:15 126 - - 104 169:16 127 3 10:55 176 300:25 128 2 4:45 158 289:55 129 6 16:00 182 229:49 130 4 10:15 144 249:48 131 2 4:35 92 147:20 132 4 8:40 125 207:42, 133 - - 9 8:17 Totals 43 96:35 2182 3 394:59 25X1` 25X1A B. OPERATIONAL SUMMARY AND PROGRESS 1. EMERGENCY CAPABILITY (SKYLARK): A SKYLARK type MPX was conducted 25-26 October 1966. This was an In-House MPX between Flight Planners at Headquarters Message exchange was limited to Mission Alert message, Mission Plan Messages, and Camera Programming Message. Canned SKYLARK departure and withdrawal routes were used with penetration route planned to cover maximum land mass. This route will be retained as a possible canned mission until such time as LLIU OAZ~' A/R areas are revised. 2. CONTINGENCY PLANNING - FAR EAST No change. 25X1A 3. 1 a. A revised Operations Plan 51-66 25X1A was published and distributed on 20 October 1966. 25X1A 25X1A TOP SECRET 2003/08/18: CIA-RDP68BOW24R00 - DEPLOYMENT PLANS: - No change. 25X1A Approved For Release 2003/08/'f - 8B00724R000 Approved For Release 2003/08 :5P68B00724R000100090031-8 Page 4 4. FORWARD BASE EXERCISE: a. The quarterly Forward Base Exercise (FBX-03) was conducted at during the period 11 through 14 October 66. The purpose of FBX-03 was to exercise forward base facilities and perform flushing/ fueling of KC-135. 25X1A b. Critique comments from all participants subsequent to exercise termination were favorable. On 25 October, a Planning Conference was convened at Project Headquarters to finalize plans for a BLACKSHIELD/ CPX to be conducted from Kadena AB, Okinawa, 25X1A Representatives from AFRDR, SAC Hqs., 903ARFS, and Project Headquarters staff sections attended this con erence. CPX is scheduled for the week of 14 November 1966. 6. A-12 DIVERSION a. On 19 October, Aircraft #125 experienced a rise in EGT followed by numerous compressor stalls requiring the pilot to shut down number two engine. The aircraft diverted to Kirtland AFB, New Mexico, and landed without incident at 1834Z. b. Pre-packed recovery kits and su ort personnel were flown to Kirtland aboard the C-130 and F-27 aircraft. Security representative and Maintenance Supervisor arrived at Kirtland 19 October/ 2100Z, to monitor the secure handling and guarding of the A-12 and pilot. A Beale AFB, KC-135 tanker arrived at Kirtland with PF-lA fuel on 20 October/2200Z. The A-12 "buddied" Iwith the KC-135 on 22 October with an F-101 -27ying e". The flight was completed without incident. 7. PROJECT PILOT INVENTORY: a. Project Pilots are currently classed as operations y ready. b. One new pilot candidate was assigned Project Pilot duties on 28 October 66. c. One new Project Pilot is under consideration with a scheduled contract date of 4 November 66. 25X1A 25X1A 25X1A TOP SECRET Approved For Release 2003/08/18 : CIA-RDP68B00724R000100090031-8 Approved For Rele4 TOP SECRET se 2003/08/18 : CIA-RDP68BOW24ROO010009003 Page 5 8. A-12 AIRCRAFT: I Iaircraft are a i ss gned to which are assigned to the Detach t men a to the Flight Test Center. Aircraft #124 is a J dual seat trainer, all other aircraft are J-58 e 9. PERFORMANCE STATISTICS: a. Maximum Speed 1. Art, #125, Flt. No. 105, 8 May 65 No . b. Maximum Take-Off-Gross Weight 123,750 lbs. 1. Art'. #129, Flt. No. 105, 8 May 65 C. Maximum Altitude 1. Art. #129, Flt. No. 138, 14 Aug. 65 90$000 ft. d, Maximum Endurance - Subsonic/Supersonic 7:40 (4 A/R) 1. Art. #127, Fit. No, 175, 18 Oct. 66 e. Maximum Endurance - Subsonic Only 1. Art. #129, Fit. No. Maximum Sustained Time 1. Art. #129, Flt. No. Maximum Sustained Time 1. Art. #129, Flt. h. Maximum Cumulative 1. Art. #130, Fit. 139, 19 Aug. at/above 3.0 130, 22 July at/above 3.2 2 nd I I -7 equipped, quipped. 3.29 Mach 5:50 (1 A/R) 65 Mach 1:17 65 Mach 1:14 130, 22 July 65 time at/above 3.0 Mach No. 54, 12 November 65 i. Average A-12 Time - Detachment Pilots j. Detachment Pilots Mach 3.2 qualified 25X1A 25X1A 25X1A 5X1A Approved For Release 2003fMfg 8S&ii fi DP68B00724 - Approved For Rele4 TOP SECRET se 2003/08/18 : CIA-RDP68Rp6724R Page 6 II. IDEALIST A. DEVELOPMENT SUMMARY AND PROGRESS 1. The initial U-2R Development Progress Report from Lockheed stated that work is proceeding according to schedule. A late November review of the basic structural design and mock-up engineering has been scheduled at the LAC facility for Headquarter's representatives. B. OPERATIONAL SUMMARY AND PROGRESS 1. GENERAL SUMMARY 25X1A a. There were no Agency U-2 overfliahts during the 25X1A month of October. Operations at the Detachment were curtailed on 17 October due to rest ent Johnson's Far East trip and the Manila Conference, bo completed requirements on 3 October for CAT status. C. I _J completed training at dwards AFB on 6 October and has returned to for local upgrading. d. System 20 tests, were success u y completed on 6 October. e. The first two flight tests for Project L_ were flown during the month. The first test was a safety which was successful. The second test prove e enough fuel data to enable the planning of future tests and operational missions on the assumption that the U-2 will carry It also disclosed a Which has since been tort c e 2. PRODUCT IMPROVEMENT a? Project flight tests were successfully performed during the month with targets covered as scheduled, 25X1A 25X1A 1X1 b. The ASN-66 tests were conducted in conjunction with the flight tests. Lockheed is preparing an ECP for procurement and installation of Doppler/ASN-66 equipment. This ECP is due in Headquarters TOP SECRET 25X1A Approved For Release 2003/08/18: CIA-RDP68B00724 - Approved-For Relep TOP SECRET se 2003/08/18 : CIA-RDP68BW724R000100090031-8 25X1A Page 7 c, The Air Data Computer/Tape altimeter tests were suspended due to the necessity of having to remove certain portions of the equipment to perform higher priority tests. Completion of the interrupted tests is scheduled during November. d. The "H" Camera, S/N 002, has been modified and interfaced with the autopilot to provide for a four- position scan and quick cage capability, Two tests were flown (26 and 27 October) with unsatisfactory results. The problem is with the take-up of material during caging. The caging action places a side load on the film during film transport, resulting in film jam, on the take-up spool: Corrections are being made and testing will continue on the first of November. e. A series of successful System 12B and 13A tests were performed during the month. The System 12B used on the 4 October test had the original ATI amplifier and antenna plate with ATC blanking, III. ISINGLASS No change. Approved For Release 209081 Eb l -RDP68BOO724R000100090031-8 25X1A ? Approva4- For Release 2003/0% : ?fcIKIffP68WO724R000100090031-8 MARD/COMPT/OSAJ Page 8 ] '(9 Nov 66) Distribution: Cy 1, 2, 3, 4 - C/P&PS/DD/S&T Cy 5 - D/ SA Cy 6 - D/O/OSA Cy 7-- D/R&D/OSA Cy 8, 9 - BPD/OSA Cy 10 - RB/OSA Approved For Release 20031081T8 : C - 68B00724R00 25X1A 25X1A 0