CABLE TO DIRECTOR FROM KWCABLE RE FLIGHTS NUMBERS NINE AND TEN WERE FLOWN ON TUESDAY 12 JUNE

Document Type: 
Collection: 
Document Number (FOIA) /ESDN (CREST): 
01425842
Release Decision: 
RIFPUB
Original Classification: 
U
Document Page Count: 
4
Document Creation Date: 
March 9, 2023
Document Release Date: 
December 17, 2021
Sequence Number: 
Case Number: 
F-2018-01483
Publication Date: 
June 13, 1962
File: 
AttachmentSize
PDF icon CABLE TO DIRECTOR FROM KW[16004132].pdf222.23 KB
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Approved for Release: 2021/11/22 C01425842 CLASSIFIED MESSAGE OATS 20002 13 JUN 62 TO D 'RECTOR MOM ITCABLE Among DPD (1,21 vii,5 p6,7118,9 10) IMF� S/C (11) Si) TOR 205 92 13 JUN 62 TO OPIM AD IC IINFO OXCART EYES ONLY FOR COI. BEERL I, MR PARANG OSKI, MR KEEFER, FROM COL NELSON TWO FLIoirs WERE FL OWN ON TUESDAY 12 JUNE, FLIGHTS NUMBERS NINE AND TEN. FLIGHT NUMBER NINE AIRBORNE ONE HOUR FIFTEEN MINUTES, TAKE.' OFF WE 'GM 85,000 POUNDS AFTERBURNER WITHOUT WATER. CLIMB 350 KEAS TO 20 THOUSAND � AB OFF, FULL DEFLECT ION ROLL AT o92 AT 20 THOUSAND. AB CLIMB TO Al THOUSAND ACCEL TO 102 MACH, ACCOMPLISHED 2G WINDUP TURNS Kr ij�THOUS AND WITH 2 G MAINTAINED IN STEADY STATE TURN, CL IMBED TO A5 THOUSAND, 270 KEAS WIND UP TURNS TO 105 G MAINTAINED IN STEADY STATE TURN, ROLLER COASTERS ACCOMPLISHED AT 5 T NOUS AND DECENDED TO i� THOUSAND, 2 TO A DEGREE SIDE SLIPS EACH WAY ACCOMPLISHED AT 250 K, THESE REPEATED AT 300K, INVESTIGATED SINGLE Al) FAILURES AT 40 THOUSAND, FEET OFF RUDDERS, RECORDED YAWING AND TRIM REQUIREMENTS, "1", ens CABLE 4978 � DESCENDED TO 30 THOUSAND, CONDUCTED STABIL IT Y 'Nast NAT IONS REPRODUCTION BY OTHER THAN THE ISSUING OFFICE IS PROHIBITED. Copy No, Approved for Release: 2021/11/22 C01425842 Approved for Release: 2021/11/22 C01425842 A. SECRET CABLE 4978 (IN 39220) PACE Two WITH CC BACK TO 25 PERCENT MAC, As YOU AWARE THIS WAS FIRST FLIGHT WITH AU. TANKS SEALED AND NITROGEN sYsTEM IN ORM ION e- ALSO, THIS WAS FIRST FLIGHT wITH ANGLE OF ATTACK AND YAW INDICATING SYSTEMS INSTALLED, ANGLES oF ATTACK FOR LANDING CONFIGURATION WERE INVESTIGATED WITH 10 DEGREE RECORDED FOR 160 KEAs AT LANDING WEIGHT" 10,5 DEGREES RECORDED FOR 155 KEAS, FOR SIMLLATION OF SINGLE ENGINE LANDING, RIGHT ENGINE WAS PILLED BACK TO 80 PERCENT RPM ON DOWN WIND LEG, LEFT ENGINE VARIED BETWEEN 96 DEGREES TO 9g DEGREES Rpm TO FLARE, THREE DEGREE TO 4 DEGREE RUDDER TRIM UTILIZED IN PATTERN To REDUCE RUDDER FORCES REQUIRED, TRIM WAS ZEROED our JUST PRIOR TO FLARE, TOUCHDOWN AT 145K, NORMAL LANDING, CHUTE DEPLOYED AT 140K, SEVERAL RISERS FAILED AT REEF POINT, SNAPPING BACK AND TEARING CANOPY IN TWO PLAcEs AT ABOUT THE 10 O'CLOCK POSITION, VIEWED FROM BEHIND, THESE TEARS APPEARED TO DE ABOUT 5 FELT IN LENGTH, HOWEVER THE CANOPY DID NOT COLLAPSE BUT CONTINUED "ro DECELLERATE AIRCRAFT, PILOT TuRNED OFT RUNWAY 32 AT TAXIWAY, AIRCRAFT WAS REFUELED AND PREPARED FOR AFTERNOON FLIGHT, FLIGHT NUMBER TEN WAS AIRBORNE FORTY SIX MINUTES, TAKE OFF WEIGHT 85,600 POUNDS Cc AT 2103 PERCENT MAC: EssENTIALLY SAME FLIGHT TEST ITEM WERE SCHEDULED, TAKE OFF NAPE IN AD PX 86 DECREES F TEMP, WITH APPROXIMATELY 7 KNOT TAILWIND COMPONENT, TAM OFF MADE ON RUNWAY 32 TO PERMIT ROLLOUT ON LAKE IF TAKE-OFT ABORTED, CLIMB WAS MADE TO 38 THOUSAND IN An, ACCELERATED To 102 Approved for Release: 2021/11/22 C01425842 Approved for Release: 2021/11/22 C01425842 SECRET CAKE �978 ( IN 39220) PAGE THREE MACH AT 40,000, TUR MD BACK TOWARD AREA IN 102G TURN ACCELERATED TO 397 KEAS AT 40 THOUSAND, CL IMBED TO 42 THOUSANDS PILOT DETECTED WHAT HE 'mown WAS EITHER MILD BUFFET OR TURBULENCE AT 1q47 MACH, IMMEDIATELY CAME OUT OF AB AND SLOWED AIR CRAFT . INSPECT ION BY CHASE REVEALED SHEET MET AL DAMAGE TO INBOARD S IDE OF LEFT VERT ICAL 300K DESCENT WAS BEGUN FOR RET URN TO BASE, REMAINDER OF FL IGHT WAS CANCELLED DUE TO ABOVE AND DUE TO CONSIDERABLE TURBULENCE AT LOW ALT ITUDE a FUEL DUMP SYSTEM WAS EXERCISED, DUMPING 10 THOUSAND POUNDS FUEL, APPROACH AND LANDING NORMAL wrril NO DRAG cHurr ABOARD . ROLL Our ON LAKE BED WAS NORMAL WITH MODERATELY STRONG BRAKING EMPLOYED LAKE BED WIT HSTOOD ROLL OUT SAT ISF ACTORIL Y. NOTED BY RUNWAY OBSERVERS WAS FACT TH2_11GIff MAIN GEM OUTBOARD TIRE WAS FLAT DURING LANDING ROLL WIT! TIRE PAICIALLY D ISENTEGRAT ING DURING - CHECK OF X RUMENrgJNJETEALED TIRE BLEW ON TAKE-OFF a WAS UNAWARE OF BLOWN TIRE UNTIL INFOR LSD DURING TAXI BACK TO HANG AR. AXING. PILOT INSPECT ION OF VERTICALS REVEALS SKIN CRACKING AND SEPARAT ION ON INBOARD SIDE OF LEFT VERTICAL JUST AHEAD OF BEEFED up AREA MODIFIED AFTER LAST PREVIOUS INCIDENT OF CRACKING, CRACK RUNS VERTICALLY ABOUT 1 INCH AHEAD OF BEEF UP AREA. INBOARD SIDE OF R IGHT VERT ICAL DID NOT APPEAR TO CRACK AND SEPARATE, BUT SEVERAL Li RIVETS WERE PULLED THROUGH THE SKIN. OUTBOARD SIDES OF Boni VERTICALS APPEARED TO BE NORMAL . FL IG HT PLANNED FOR WEDNESDAY WAS OF COURSE CANCELLED. IT NOW, APPEARS THAT THURSDAY FL IGHT WILL ALSO BE CANCELLED DUE TO ABOVE PROBLEM PLUS A POSSIBLE ENG INE CHANGE. revtir Approved for Release: 2021/11/22 C01425842 Approved for Release: 2021/11/22 C01425842 SECRET CABLE 4978 (IN 39229) PAGE FOUR INFO ON ENGINE CHANGE REQUIREMENr WILL DE FORWARDED WHEN LTAILS ARE CLARIFIED. COL DEERLI PERSONALLY BRIEFED PRIOR TO DEPARTLRE. END OF isssAGE SECRET Approved for Release: 2021/11/22 C01425842