CONTRACT AF33(600)40280 WESTINGHOUSE REFERENCE: DYD-45196

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Document Number (FOIA) /ESDN (CREST): 
CIA-RDP67B00657R000200210016-6
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RIPPUB
Original Classification: 
K
Document Page Count: 
32
Document Creation Date: 
December 22, 2016
Document Release Date: 
December 9, 2010
Sequence Number: 
16
Case Number: 
Publication Date: 
March 23, 1965
Content Type: 
MEMO
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PDF icon CIA-RDP67B00657R000200210016-6.pdf2.03 MB
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Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Westinghouse Electric Corporation Air Arm Division Friendship International Airport Box 746, Baltimore 3, Md. Telephone: 761-iooo 23 h1 -Of ntft0b, We STAT STAT Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 &' osm-w Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 V1 L-W.F,L- of 110w "Nor %OOF gr Copy 2 of 6. PROGRESS REPORT FOR PERIOD OF SEPTEMBER 1, 1964 TO JANUARY 31, 1965 CONTRACT NUMBER AF33 (600 )40280 BY WESTINGHOUSE ELECTRIC CORPORATION AEROSPACE DIVISION BOX 746, BALTIMORE 3, MARYLAND 21203 S'' .CIA.L HANDLING Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 TABLE OF CONTENTS PROGRAM A F-1O1 FLIGHT TEST . . . . Modification & Ground Test In-Flight Tests . Instrumentation . . . PHASE II FLIGHT TEST . . . . . . . . B ~y ~}~{ DYNAMIC ~~ C I NAMIC CORRELATO ONMENTAL TEST . 9 10 EQUIPMENT MODIFICATION . . . Low Noise RV Pre-Amplifier 14 ange Boost . . 15 Increased Power output . 16 SYSTEM . 16 Receiver Phase Shift 16 Recorder . . 19 Reliability . . 19 H GROUND SUPPORT EQUIP? I SPARES . APPENDIX Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 A F-i0l FLIGHT TEST The 300 hour periodic inspection of the F-101 aircraft was completed with the functional test flight on 9 September 1964. The first radar flight followed on 14 September. A summary of the flight program is given in Table Radar flights flown in this period from September 1964 through January 1965 are summarized in Appendix A. A defective aircraft cooling system prevented flights between IT December and 28 December. Modifications and Ground Tests Receiver Three receiver modifications have been performed and tested. First,, the Tunnel Diode Pre-amplifier was replaced with a parametric amplifier built by Micro-Mega, repeating a test started on fligh 114 prior to the aircraft inspection. This amplifier has gain of 16 db and produced a system noise figure of 5,6 db, an improvement of 0.9 db over the Tunnel Diode Amplifier. After flight testing on 127, the TDA was re-installed. Prior to flight 130, a second lim amplifier was in- stalled to allow cockpit variations in the signal level to the video amplifier without changing the limited signal to the DST. This permits changing the signal return power at which limiting occurs. This second limiting TF has remained a part of the F-10l installation. The third receiver modification consisted of replacing the Tunnel Diode pre-amplifier with the final configuration of the parametric amplifier, one designed and built by Westinghouse. Installing this component required constructing a 400 volt power supply, Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 TABL P-101 PROGRAM SUMMARY September 1964 through January 1965 Flights Scheduled Flights Accomplished Aircraft Functional Feet Flight Pilot's Proficiency Radar Productive Flights Productive Flights Prior to a Failure Film drive and diode switch failure Transmitter overload Transmitter failure Transmitter servo failure No Results Film drive failure Military Operations over target area 1 Cancelled Weather Motion Compensation System Transmitter Transmitter Servo Aircraft Compass Problems Aircraft Oxygen Supply Inadequate Aircraft Turbine Failure Inspection Scheduling 24 19 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 ,J7 `v.. .r -- -- fabricating and mounting bracketry, and modifying wave-guide runs. This par-amp produced a system noise figure of 5.1 db, and is now installed and ready for flight test. Because of the improved noise figure and apparent stability of this unit, units of this type planned for the two deliverable systems as well as the F-1O1. Receiver tests performed on the P-101. system were reported STAB 164. Transmitter Flights ~hrough 123 used a transmitter having a narrow pulse forming network in the CPA discharge circuit. Pulse width was 28 nanoseconds and average power 22.5 watts. The remainder of the flights used the original PFN, which produced 37 nanosecond pulse width at 29.5 watts. The narrow transmitted pulse generated by reducing T WT NP drive pulse width (as described in section Z this report) has not been flight tested. Prior to flight 132, the thyratron was replaced in the CPA modulator and average power increased to 58 watts. TWT and CFA pulse coincidence was lost on flights 120 and 121, caused by a defective tunnel diode in the transmitter servo. Checking to determine if temperature was a problem, a thermistor measured the highest temperature on the servo chassis in-flight to be 39?C, which is not excessive. Doppler Frequency Tracker Six flights, were made off -shore from Charleston, South Caroline o savannah, Georgia. For the last four of these flights, the DFT gate was moved from its normal 180 use o range to 235 uses to reduce the lose of DFT operation when the gate is over water. _5_ Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Motion Compensation Tests on the motion compensation system were started on ight 117. In-flight the integrator output would not return to zero. This condition was corrected by changing tube and wire shield grounds and by adding decoupling to the power supplies. In addition, a transient occurs when the accelerometer is connected in-flight to the integrator network,, pausing the network to accumulate an excessive charge. Investigations into this network charging are still underway. During the course of these tests, an integrator of deliverable configuration (built by Minneapolis-Honeywell) was installed in the F-1O1. After correction of initial drift problems, satisfactory operation was obtained. System gain was checked by causing the aircraft to pitch sinusoidally approximately 4.3g and evaluating instrumentation data. Results were obtained on the film of flight 131 with the forced aircraft pitching both with and without motion compensation. An incorrect accelerometer scale factor (volts per g) caused the gain at the integrator input to be set too high on flight 136. Recorder The film speed inverter and CRT filament power supply have been installed external to the recorder to minimize 400 cps pick-up. Following flight 126, a general tightening of the recorder was performed, which improved the reliability of film transport and vibration striping on the film. This procedure is required to be repeated periodically. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Several different film emulsions of the Eastman 5401 have been used during this 30 flight period. Prior to the use of a new emulsion, sensitometric measurements and CRT bias-density curves are plotted to determine optimum CRS' operating voltages. This procedure along with a bias only film sample on each pre- flight test has enabled determination of C: performance for each flight. A defective CRT bias pot was located through these tee Recorder 007 was modified to the final altitude ( ke sweep rate) configuration and tested on flights 142, 143, and 144 to simulate final altitude results. Recorder operation was satisfactory. A study of CRT bias tests resulted in adjusting the CRT closer to out-off for all flights after 133. This theoretically (1) operates the CRT in a more linear region of the video- transmission curve, causing fewer images (2) gives greater contrast for small targets gives brighter image on the correlation,, or allows operation of the correlator at a faster speed. Results on the correlated film are signifioantlyr improved with the lower bias voltage. Nominal density on the primary film averaging about 0 3. poor correlation of flights 128 and 129 flown at the extreme lower limit of ground speed triggered ground tests of ground speed- film speed tracking. Tracking was found to be 3 per can at the lower limit of 750 knots ground speed. After ad justment, less than ,3 per cent error in film speed was found over the full range 780 to 900 knots ground speed. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 The field flattener in recorder 007 for the far range sector eked. Since useful video occurs only on far range in 4 ko ep rate operation from 45,000 feet altitude, the recorder as modified to interchange the near and far range traces on the CRT and satisfactory operation was obtained. Dual Altitude Operation Flight 132, planned for 45,000 feet altitude over Norfolk, was aborted due to military operations taking place in the flight area. Following this flight, a switch was installed in the cockpit to permit the radar operator to select D FT gate position and record blanking for either high or low altitude operation. This flight has been used twice to date to fly both high and low altitude flights the sane day. 'light Tests Repeated runs over the same target area with various second amplifier bias levels were made to determine the extent of images caused by IF limiting. Flight path was not consistent enough to check data; the series will be repeated. Several flights were flown to test the range boost circu in both the 8 ke and 4 kc sweep rate configurations, as noted in Appendix A, Four flights were made over the Philadelphia area to show results under simulated altitude conditions. A comparison of the results of flights 137 and the first run of flight 138 showed the simulation to be logical when extended to 90,000 feet, in fligh 1P2 and 143. :L H 111 U 6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 WKIAL HANULIiyu Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Altitude Recorder RF fight Simulated Sweep Rate Attenuation 142, 14'3 22,000 45,000 145,.000 45,000 145,000 90,000 4 kc 4 kc 10 db 0 db instrumentation The CEC oscillograph was removed from the aircraft in preparation for installing a KA-45 aerial camera in that location. Some of the signals formerly recorded on the CEC were added to the magnetic tape ording. The signals now recorded during each flight are: Variable Frequency oscillator Potentiometer Position Antenna Accelerometer Output Antenna Accelerometer integrator Output Antenna Position Error Aircraft Pitch Angle DFT Meter Aircraft Drift Angle Aircraft Roll Angle Antenna Roll Table Position Aircraft Ground Speed Sine of Aircraft Heading Recordings of the aoceleratlons at the location of the aerial camera were taken. -9_ Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 PHASE II FLIGHT TEST The unsolved problems listed in the August report have been corrected during this period. The errors in the INS output signals of drift and pitch were caused by loading of the INS output signal due to a wiring error in the aircraft magnetic recorder. A defective charging choke caused the transmitter overloading problem and was replaced. The erratic pulsed 120 me from the frequency generator was due to a malfunction in the crystal gate driver. Because of the lull In the Phase II activity, the following was returned to Baltimore in October to increase the assistance to the F-201 Flight Test Program and provide a back-up system: (1) three of the four field engineers adar system 002, not including the antenna and single axis platform Radar Test Set valuator few pieces of standard test equipmen The second radar system, test set and the test equipment were up in a new laboratory in the hangar, adjacent to the F-101. Maintained in a ready status, this system has been able to supply replacement assemblies for the F-101 system. In addition it has been used for check-out of modified and repaired sub-assemblies. Special system tests have been performed on system 002, such' as phase-shift measurement of the receiving chain and modification of the recorder to the 4 ke sweep configuration. of the one system, activity on system 003 at the Phase II ing site has been limited to the installation of modifications on the inverter, torque motor, and focus power supply. aye~+r a. oo ai asLB~si3 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 A pressure test of the antenna indicated leakage to be about the same as it was when shipped a year ago. A fourth field engineer, normally located at the Phase II returned to Baltimore for the month of December to ass in the correlator set-up and become more familiar with the ations and testing procedures. Minor modifications to all three systems have been progressing satisfactorily. Status is as follows: Modification 'Video Amp, Increased Bandwidth Control Panel, Second Failure Determination Frequency Generator, Temperature Stability, etc. Frequency Generatorr Oscillator Transmitter, TWT Filament Supply 2 Range Mark Selector :'der, inverter Recorder, Focus Power Supply Recorder, Torque Motor Recorder, Inverter Low Frequency Cut Out C DYNAMIC CORRELATC)R 1 N/A N/A N/A N/A N/ N/A The dynamic correlator was transported from the Phase II testing area to Westinghouse. After arrival in Baltimore on November 23, th correlator was set up in a special laboratory space, with the first correlation processed on December 11. Operation of the equipment Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 by the same two Itek representatives as previously, with results that are equal to those attained previously. Initial installation was with a makeshift exhaust blower. After installation of the proper blower and correction to the conditioning in the room, a positive pressure in the room was attained. Dust studies under various conditions are being conducted reduce the level as much as practical. In January a Contact Printer was received as OFE and set up in the same laboratory as the correlator. Itek personnel 0 most of the operation with this printer. Dupes of both the primary correlated films can be exposed with this printer and developed with the Veers mat provided by Westinghouse. The consolidation of the radar and correlator work at Westinghouse has reduced the time to process flight films. However, erplay between the personnel of the two equipments is of much more significance. Several instances have occurred in the two months of operation where both radar and correlator problems have been engaged more productively with the close coordination now possible. First example came with the processing of flight 136 film. First correlations were out of focus. However, a refocusing of the correlator produced good results and pointed out the eexceseit of change of the Variable Frequency Oscillator by the accelerometer integrator. Further checking isolated the difficulty to the wrong scale factor used for the accelerometer. More recently, ground speed and imaging problems have been eked more imaginatively through short recorrelationa of certain ;ht or test data film. As both the radar and correlator engineers become more familiar with both equipments, even more Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 ive use of the equipment can be made. Advantages to the Radar Interpretation program of this correlator location are just as great. D ENVIRQNM N'AL TEST The results of the temperature and altitude tests on the Frequency Generator were released In January as STM 161 environmental tests in addition to this were performed durini period. ICATION duced Transmitter Pulse Width ahoratorr work on reduced transmitter pulse width was completed, using the rack breadboard traner urned from S FD. Transmitter results were encouraging, while receiver response revealed an inability to reproduce the narrowed pulse. Changing the CPA pulse forming network from 30 to 20 nano- ends did not narrow the output pulse because of stray capacitance of the charging choke and filament transformer. A 20 nanosecond output pulse was obtained by narrowing the TWT RP pulse driving the CPA to 20 nanoseconds a normal anode pulse. pulsing the CFA with A CFA tube which delivered 146 watts average, 1. MW peak, 30 nanoseconds, generated 90 watts average, 1.1 MW peak, when operated with a 20mnoses and TWT pulse, Modulator efficiency dropped 26 per cent due to the increased effect of stray capacitance at the narrower pulse width. Receiver response tests showed that the video output pulse owed only slightly (approximately 3 per cent) for the 33 per cent pulse width reduction from 30 to 20 nanoseconds. At the same -13- Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 the amplitude decreases by 1.8 db. Thus, the present receiver prevents taking full advantage of the narrow pulse widths attainable with the transmitter. Low Noise RF Pre-Amplifier A wideband non-degenerate parametric amplifier was designed J:GL L.L.Lgm, Tr e' a-u:Lng in to F-iO"1. This Parametric amplifier uses two matched varaotor diodes in a novel circuit design to achieve improved temperature stability. cult configuration permits easy tuning of the idler resonant frequency, eliminating the idler frequency from the signal Stringent phase requirements between pump and signal frequent are eliminated. The delivered parametric amplifier, to be Installed in the F_101, has the following characteristics: Noise Figure Gain Bandwidth, 3 db 1 db Flat Insertion Lose with no pump power Pump Power Pump Frequency Beam Supply Reflector Supply Bias Supply 3.6 db 16 db 270 me 0 me 3 db 135 milliwatte 25,01 gig xycles -1039 volts at 28.5 milliamps 769 volts 0.545 vol Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 System noise figure should be improved 1.0 to 1.5 db over that attained with the Tunnel Diode Amplifier. Further Improve- ment (about 0.3 db) could be attained by using a low noise second stage in place of the present TWT. Parts are on order for the two deliverable pre-amplifiers, geBoost Range boost extends the high frequency response of the video amplifier to compensate for the recorder high frequency response. Test films were generated using a single pulse in range of 20 to 40 nanoseconds duration. Four degrees of high frequency boost were run for each pulse width. Evaluation of the resulting was accomplished by scanning the recorded signal on the primary film with a micro-densitcmeter. Rise time of the recorded pulse was improved with range boost, but it was accompanied by ringing of the range pulse. Effective range resolution was not Improved with any of the four amounts of boost. The preceding ground tests were performed on recorders of both the 45,000 (8 kc sweep rate) and 90,000 (4 kc sweep rate) foot configuration. Little difference was noted in the results of the two recorders as predicted theoretically. The work is complete except for the detailed evaluation of the 4 kc microdensitome scans. Data flights were made in the F-101 using the range boost of our degrees with both the 8 ko and 4 ice recorders. prove meat of range resolution was noted on the secondary film. As a result of these tests, the two deliverable systems will not be ed for range boost. -15_ SPECIAL H AN OLIN G Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Increased Power Output has been recommended that the proposed modification of increasing power output by using improved cross field amplifier tubes be deleted. The expected improvement of 1.5 db in signal- to-noise ratio by this high power modification is about the same Improvement attained through the change from a tunnel diode to a parametric pre-amplifier. The cost of the high power components alone would be more than the cost of the complete parametric amplifier installation. In addition, it is expected that normal tube development will make higher power CFA tubes available in the future. Receiver Phase Shift Phase linearity measurements were performed on the system receiver. Tests were performed using both the regular video of the tests are shown on the graph of Figure 1. Referring to the test equipment arrangement in Figure 2$ the signal source was an X-band klystron, whose output was fed to TWT. This TWT was serrodyned to add 1 ko to the test signal, and its output passed through the receiver. The klystron test frequency also passed through a phase shifter and double mixed in order to beat the video amplifier output frequencies down to a difference 1 ko, containing the system phase information. The serrodyning process produced some discontinuity pips at the 1 ko rate. These pips were reproduced at the output of the balanced and served as phase change markers on the scope presentation. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 TESTJAJC7 LLVSTI UN r t I ~ } 9b /Sc ~7? 3bo DE4'REE i 7b Ifw AWN. W. SC' L 14 e$'E,/IATio#/ Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 VZCZ . PRK/S/cx/ PN49g SH/r7Ei2 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 A low pass filter removed the pipe on the scope sync input, allowing the scope to sync on the sinewave only. Thus the pips were caused to move across the scope face in response to the system phase function. Results with the wideband video are a smooth linear curve with a one cycle superimposed ripple. Origin of the ripple was not determined. Deviation in the phase shift of the receiver with -band video amplifier was within acceptable quenc lea s up to 20 me. Recorder video Analysis and some laboratory effort was performed to determine techniques of speed-up and linearization of the recorder sweep. Both are required to match the correlator characteristics and im- prove the output resolution. No changes are planned for this generation of equipment, since the improvement In resolution is rather small considering the cost Involved. lability, Failures have been reported through procedures established in February 1964 which allow calculation of mean times between es for these systems. All improper system operations are classified as failures, including film Jams, broken wires, and operator errors. Failures in which more than one component fails are considered only a single failure. The I" SF calculations are weighted to reflect actual ratio of standby to transmit time. A summary of the failures and ? BF calculations is given below for the system in the F-101 and system 002, just recently returned to Baltimore. Operating time on system 003 in the field has been too low to make valid calculations -19- Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Period P-101 system 2/4/64 to Operating Time, Standby 566. Transmit 140.5 Average Standby 48.2 s, Receiver 2 Recorder power Supply Synchronizer Transmitter Nav Tie Miscellaneous but there was excessive flow into the slots during the pressure cure and a losses of strength of the bond. Various batches of Doryl from the two available sources were tried with varying results. Acetonate to the Doryl adhesive caused a brittle bond with little adhesion. Aerosol OT was added to the adhesive as a wetting agent System 002 1/25/65 4/3/614 to 1/21/65 23T-7 32.1 24.4 0 7.2 Although all tests on antenna pressure sealing have not been successful, the latest results are encouraging. Adding Ferric Acetel Mean Time Between Failures 4 ANTENNA these months of experimentation, best results were obtained when using production Dory?. Power bubbles resulted when the cure cycle started with a cold oven. Acceptable adhesion can be achieved only when the array sticks are post cured for three hours at 315?C. Since the solder sealing the module assembly ments at 310?C, the modules must be disassembled, bonded and reassembled. -20- Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Rework of Antenna 3 was started. During this rework, it was found that the bubbles generated in the bonding operation could be reduced significantly by perforating a row of .030 diameter ho along each edge of the 18 fabric and in areas not covering the slots on 40 sticks indicate 75 per cent of the sticks have pressure within acceptable limits on the first bonding attempt. Those sticks out of tolerance have been reworked successfully by cv coating with 16 resin. e end of January, three modules of 16 sticks each have been dismantled, aned, vapor blasted, and ultra-sonically cleaned. Bonding is complete on two modules and their reassembly started. H GROUND SUPPORT EQUIPMFM At the completion of the recorder development, Itek supplied a rack used to test recorders. Changes were designed to allow this rack, when used with the standard test equipment, to perform the functional tests independent of the system on all radar system assemblies, except the transmitter and single axis platform and its electronics. A few power supplies, control circuits, and cables ation approximately 85 per cent complete quired. Design of the changes are complete, and the actual The recorder cart is complete and now in use with System 002 in the hangar. A review of the Film Evaluator suggested several improvements in the azimuth evaluation portion to improve the usefulness in the examination of test targets. The following modifications were undertaken t Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 (1) add enter to source slit to allow setting repeatability trengthen mechanically the track for the scanning (3) modify projector section, using better lenses in an arrangement which allows easier and more stable alignment 4) modify phototube circuitry to provide logarithmic display (5) modify the light source to improve alignment and stability. All the items have been completed, axe The Radar Test Set has been used extensively to provide is to both the System in the F-101 and the back-up system. Particularly useful is the dual azimuth target simulation, as used in the tests to determine the effects of receiver non-lineariti I SPARE During this five month period, 68 items of system spares have been shipped, leaving 54 open items. Of 8 added to spares during this period 33 were transferred from the cu sser supplied list to be Westinghouse supplied and 11 were increased quantities. Completion of spares work by amendment is as follows: ems PerCent Complete list plus first 7 amendments Amendment 8 Amendment 9 Amendment 10 18 2 98.5% 56 % 0 % On the spares for Ground Support Equipment, 14 items were shipped during this period, no items were added, leaving 15 items remaining to be shipped. This amounts to 97% completion of the OSE spares. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67BOO657ROO0200210016-6 APPXNDIX A SIC OF FLIGHTS Flight Number 115 116 117 Date 9/14/64 9/16/64 9/23/64 Altitude 22, 500 22,500 22, 500 Area Philadelphia, Pa. Norfolk,. Va. Washington, D.O. Purposes System checkout and data Data acquisition and range Test range boost with 3 IF -acquisition. boost tests. gains and linear motion compensation system. Significant 30 V P-P limited video. 30 V P-P limited video. System Changes Results Presentation good from 1/2 Presentation fair in best Presentation on a 50 sec. to 3/4 range. Resolution areas. Imaging and clutter length of WF2 is fair. WF1 in best areas about 15 ft. detract significantly. Vege- is too dense and lacks con- in azimuth and 20 ft. in tation clutter extends into trast. Imaging of a bridge range. Clutter present on water. Contrast and resolu- is present. There was an all strong targets. Images tion in best areas fair. No apparent reduction of trans- present on same. Contrast discernible effect of range mitten-receiver isolation irly good. boost. Focus poor over during flight. Film failure near range. during Run #2. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67BOO657ROO0200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Flight Number 118 119 120 Date 10/l/64 10/6/61+ 10/9/64 Altitude 22.500 220500 1+5,000 Area Washington, D.C. Washington, D.C. & Philadelphia, Pa. Baltimore., Md. Purposes Test range boost with 3 IF Test range boost with 3 IF Test linear motion ccmSpensa- gains and linear motion gains and linear motion tion system and range boost 5. compensation system. compensation system. Significant 12.5 V P-P video noise. System Changes Results Presentation is good from Presentation is good from For about 8 clocks the 1/2 to 3/1+ range except 1/3 to 3/4 range (on Run presentation was fair over some empty gaps in azimuth -11 at 10 volt level)o a strip from 1/2 to 3/4 due to transmitter failure. Best azimuth resolution range. During part of the 5 Volt signal level appeared is approximately 15 ft. flight transmitter was out better in contrast than 10 Low level contrast is of coincidence. 400 cps or 20 volt level. No dis- good over best areas. images were strong during cernible map differences Imaging and clutter is this time. in range boost changes. seen by strong targets as bridges., particularly from clocks 62 to 64. Good detail on most of map. No correlated film at 5 volt level. Transmitter failed during flight. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Flight Number 121 122 123 Date 10/13/64 10/16/64 10/21/64 Altitude 459000 22,500 229500 Area Norfolk, Va. Western Maryland Boiling ~T Washington., D.C. Purposes Test range boost 5 with Test range boost against Test range boost against variable receiver gain. corner reflectors. corner reflectors. Significant Selected video noise Reduced recorder bias from System Changes levels of 20 Vp 17 V, 38 V to 30 V. and 12 V. Results Map is fair for first Weather prevented flying Map fair over strip from 1/2 3-1/2 minutes over a strip by corner reflector area. to 3/4 range. Corner re- from 1/2 to 3/4 range. Map is poor over the best flectors appeared on poor Remainder of roan has too regions. Contrast and part of map on all runs. low density and poor con- density are too low. Over Azimuth resolution from de= trast. imaging at 400 part of the film the tailed correlation of red cps was strong. Even density is so low that flector areas was 3 to 4 ft. shore extends into water strong targets are hardly No range boost effects dis- rather strongly. identifiable. cernible. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 -4- Flight Number 124 125 126 Date 10/28/64 11/4/64 11/10/64 Altitude 459000 459000 229500 Area Norfolk,, Va.. Philadelphia,, Pa. Purposes Data acquisition with re- Test new linear motion Test linear motion compensa- flectors at Norfolk Air- compensation system. tion system. port. Significant PFN change resulted in Minneapolis Honeyvell System Changes pulse width of 37 usec. Integrator installed and 29.5 watts pop. prior to flight. Results Far range strip is good On far range strip map is Film jam in recorder pre- over most of the range. good from 1/3 to 7/8 range vented acquiring data. Contrast is fair. Near over most of the flight. range is good from 1/3 On near range strip map to 3/4 range. Imaging was good from 1/2 to 2/3 at 400 cps not as strong range. Lox level con- as in some previous trast is only fair. flights. Resolution in Imaging of bridges is azimuth is approximately quite noticeable at 25 ft. spacings of 400 cps, and 120 to 150 cps. Compen- sating effect of ac- celerometer is not ob- vious. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 -5- Flight Number 127 128 129 Date 11/13/64 11/17/6+ 11/17/64 Altitude 45,000 45,000 45,000 Area Norfolk, Va. Charleston, S.C. Charleston, S.C. Purposes Test micro-megs parametric Data acquisition. Data acquisition. amplifier. Significant Parametric amplifier in- TDkre-installed prior System Changes stalled for this flight. to this flight. Noise Noise figure 5.6 from figure 6.5 db. 6.3 db. Results tap was smeared in azimuth Map out of focus entire fl ight. Inconsistent drift data and contrast poor over whole from doppler navigator over smooth water causes doubt in flight. Flight was rough. ground speed data. Many b ank spaces occurred because of Since accelerometer was IFT unlocking. Water was i maddy. Resolution poor. not used in motion compen- sation, film was badly degraded. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Flight Number 130 131 132 Date 11/20/64 11/24/64 12/7/64 Altitude 22,500 22,500 45,000 Area Washington, D.C. Washington, D.C. Norfolk, Va. Purposes Test effects of IF limiting Data acquisition and test High altitude test of in- and IF gain. integrator calibration. tegrator and data acquisition. Significant 30 V P-P limited video; 5, Auto-correlator installed Integrator re-calibrated System Changes 10, 15, & 20 db IF attenu- for this flight. prior to flight. Transmitter ation steps. Installed sepa- repair produced 58 watts pwr. rate limiting IF for signal yeah V. bias reduced Results M p is good over the range First 22 clocks taken over Military operations over strip usually in focus for rural area with only fair target area prevented super- Runs #1 and #+. For at- contrast and boundary sonic flight. Integrator in- tenuations of 10 db or resolution. Where aircraft strumentation run made at more, the density level was forced into sinusoidal low altitude. was too low and contrast motion, the map appeared was not as good as in the good (azimuth resolution other runs. 20 ft. or less) when ac- celerometer was engaged. When accelerometer was dis- engaged, periodic smears were obvious. This effect was much greater on strong distinct targets than on vegetation areas. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Flight Number 133 134 135 Date 12/9/64 12/15/64 12/15/64 Altitude 45,000 45,000 45,000 Area Philadelphia, Pa. Charleston,.S.C. Charleston, S.O. Purposes Integrator test and data Data acquisition. Data acquisition. acquisition. Significant Increased CRT bias to System Changes 37.5 V with 25 V P-P limiting video. IPT gate at 235 Usee. Results General appearance of map Strong headwind kept groun L speed 10% below nominal. In- was poor. Low level targets correct speed ratio-caused nap to be out of focus on entire hardly discernible to clock flight. Results s3mil flights 128-129, except signal #19. From clocks f25 to level more consistent. #30 astigmatism (or rota- tion) was bad and range resolution was poor. Cross track velocity was over- compensated. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Flight Number 136 137 138 Date 12/31/61 1/6/65 1/6/65 Altitude 45,E 45,E 22950? Area Philadelphia., Pa. Philadelphia., Pa. Philadelphia, Pa. Purposes Data acquisition. Reference for altitude com- Run #1 - Simulated 1+5,000 parison. flight flown at 22,500. Run #2 - Effect of 10 db SIN improvement. Significant Calibrated film speed Recalibrated integrator for Ferrite attenuator installed System Changes prior to flight. Video 5 V.G input. D]'T gate at in receiver line, controlled limit level of 30 V P-P. 235 uses. from cockpit. Results Contrast was fair and Nap improved in contrast Map is best from 1/2 to ex- resolution was between 20 and greater areas of well treme far range for Run #l. and 30 ft. in best areas. resolved targets. Some Contrast and resolution are From clocks #26 to #30 fading occurred between good. Some fading from map faded because of clocks #12 and #30 during clock #35 to #40 when antenna extreme position of an- which antenna was in ex- was in extreme position. tenna due to acceler- treme position. From Some imaging and clutter of ometer overe. sation clock #12 to #15 slope strong targets are noticeable and excessive ringing of accelerometer inte- on Run #2. of accelerometer in- grator output was ex- tegrator. Strong targets cessive. were poorly resolved in this region. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 -9- r C; Flight Number 139 i10 141 Date 1/12/65 1/12/65 1/12/65 Altitude 459000 45 9 000 229 500 Area Charleston, S.C. Charleston, S.C. Targets of opportunity be- tween Charleston & Baltimore. Purposes Data acquisition. Data acquisition. Data acquisition. Significant IPT gate set at 230 usec I gate set at 230 usec System Changes for this flight. for this flight. Results First correlations were a of focus, similar to flights From clocks #15 to #20 map 128-129 and. 134-125. Rec elated with a 20% shorter is good and resolution is focal length gave very goo - map. No explanation for good from 1/2 to 3/4+ range. error; speed ratio checked within limits from films. Average density is high and Resolution about 15 ft. azimuth and 20-25 ft. in contrast is marginal in low range in last part of 140. Contrast is good over level areas. Shore s=eared entire film. Occasional 4 DO cps and other images. into water at about 400 cps at clocks #24 and #+k. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6 Flight Number 142 14+3 144 Bate 1/19/65 1/21/65 1/25/65 Altitude 15,,000 45F000 45,ooo Area Philadelphia,, Pa. Philadelphia,, Pa. Philadelphia., Pa. Purposes Simulated 90,,000 flight; Simulated 90,,000 flight Range boost test on 4 KC from 1+5,,000a from 45,,000. recorder (007). Significant Recorder 007 modified for Replaced CRY' bias pot and System Changes 4 KC operation. set for 60 V bias. Results Defective CR1 bias pot Primary film density satis- Mip is best from 1/4 to 1/2 caused primary film factory. Best part of the range. Azimuth resolution is density to be high. Best map is from i/4 range to below average over all the part of map is near mid- mid-range due to filter map. From clocks #10 to #15 range. Average density slope mismatch. I&Lp of some azimuth degradation oc- is low,, thus contrast small tanks at clock #27 curs while integrator output is not adequate. Azimuth is good. 'lank size scales slope is greater than 25 cps/ resolution is poor over from 25 to 30 ft. on radar see. Contrast is fair for most of the map. map compared to actual first 5 clocks and better tank size of about 20 ft. during the remainder of the Motion disturbances low flight. Motion disturbances here during this view during the flight were time. Contrast is fair significantly above average. in tree-grass regions. Sidelobes or images appear at clock #32. Separation is 75 mils. Sanitized Copy Approved for Release 2010/12/09: CIA-RDP67B00657R000200210016-6