SUMMARY REPORT ON TASK ORDER NO. LL

Document Type: 
Collection: 
Document Number (FOIA) /ESDN (CREST): 
CIA-RDP78-03639A001300140001-5
Release Decision: 
RIPPUB
Original Classification: 
S
Document Page Count: 
22
Document Creation Date: 
December 22, 2016
Document Release Date: 
September 20, 2011
Sequence Number: 
1
Case Number: 
Publication Date: 
November 30, 1960
Content Type: 
REPORT
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PDF icon CIA-RDP78-03639A001300140001-5.pdf1.28 MB
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Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 SU1v 4ARY REPORT November 30'. 1960 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 This summary report describes the effort performed under Task Order No. LL, from October 14, 1959, through November 30, 1960. The objective of this program was to conduct additional research directed toward the development of a 12-month time-delay device utilizing silicone fluid that had been evolved previously, and to prepare and evaluate four timers. Background Information During the past several years, a search by many organizations for a cheap, reliable, and reasonably accurate time-delay mechanism has led to the consideration of silicone fluid as a timing medium. Under Task Order No. J, basic design criteria were established for an experi- mental time-delay unit which utilized silicone fluid. The effort under that Task Order was directed toward the development of an experimental unit for use in providing time-delay periods ranging from 15 minutes to 2 months, at temperatures varying from -20 to +120 F; the desired accuracy was such that the flow of silicone fluid could not vary more than ?10 per cent over this range of temperatures. In the research performed under Task Order No. J, it was found necessary to incorporate in the experimental unit a device designed to provide temperature compensation, so that changes in the viscosity of the fluid that were brought about by temperature varia- tions would not cause the fluid-flow rate of the experimental unit to vary beyond the specified limits. a ,FAL Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 On March 27, 1959, an effort under Work Order No. IX, Task Order No. CC, was undertaken, to conduct research directed toward the and relatively small; and was to be self-contained, i.e., emit no silicone fluid to the ambient water. Since the service environment for the desired timer would minimize temperature fluctuation, it appeared likely that a study directed toward the development of a suitable device using silicone fluid would not have to include consideration of means for temperature compensation, with its associated complexities. The Work Order No. IX effort resulted in an experimental device which showed satisfactory operating characteristics over a period of 3 months (the longest period possible within the time limit of the contract) at an ambient temperature of approximately 75 F. Because a major problem in the development of any time-delay device is reproducibility, Task Order No. LL was subsequently initiated to provide for minor modifications to the unit developed under Work Order No. IX, the preparation of four timers of that type, and an evaluation of the timers at temperatures of about 75 and 40 F. The research performed under Task Order No. LL is described in the following. Summary Under this program, the experimental time-delay unit which had been developed and evaluated cursorily under a previous research program Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 -3- was redesigned, and four timers were fabricated and assembled. The regulating or metering tubes for these timers were selected on the basis of the flow characteristics of the tubes; these characteristics were determined by metering the silicone fluid, Viscasil 500,000, through the tubes for approxi- mately 21 days. The timers were evaluated at about 75 and 40 F over a total period of about 9 months. The results obtained during the first 5 months of the evaluation period were partially invalidated by the presence of foreign particles in the fluid; lint-like particles generally restricted the flow of fluid in the timers, and in one unit, plugged the metering tube. Filtered silicone fluid was subsequently used in three of the units, in the evaluation at 40 F. The evaluation test on the fourth timer was continued through the temperature transition from about 75 F to 40 F; this unit had shown a reasonable flow rate at about 75 F, and it appeared desirable to observe the effect of the temperature change on the fluid, and consequently on the operation of the unit. The 4-month evaluation at 40 F indicated appreciable variations in the flow rate obtained in the four timers. The reason for this varia- tion was not completely apparent; however, it was believed that "dirt", i.e., foreign particles picked up during normally careful handling of the fluid and of the units, probably was the cause of the variations in flow rate. It appeared that the next logical step in the development of an appropriate time-delay device of this type would be to investigate practical methods of cleaning the silicone fluid, preparatory to performing evaluation tests on the timers filled with cleaner fluid. Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Engineering Activity The engineering activity under this program included the redesign of the experimental time-delay device developed previously, the investigation and selection of timer metering tubes, the fabrication and assembly of four timers, and an evaluation of the timers at about 75 and 40 F. Redesign of the Timer The experimental timer- developed under Work Order No. IX, Task Order No. CC, was redesigned to utilize an 0-ring seal at the flanges (between the end cap and the housing), castings for the major components, and threaded ends for connection of the unit to the workpiece and to the neutral-buoyancy chamber. A disassembly view of the modified experimental timer, without the main spring (and firing-pin mechanism), is shown in Figure 1. The flange of the rubber Bellofram piston seal was bonded to an aluninu:r_-alloy washer with an adhesive, so that this subassembly could be installed as a unit between the flanges of the end cap and of the housing. An 0-ring seal was incorporated in a face groove provided in the end cap, to seal against the aluminum-alloy washer of the Bellofram subassembly. With this seal, the flange screws could be tightened to "bottom out" the flanges, and then the 0-ring squeeze would produce an effective seal. A flat-gasket-type seal had been used previously between the flanges, and The design details were presented in the "Summary Letter Report on Work Order No. IX, Task Order No. CC" dated July 26, 1959. Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639A001300140001-5 A 1) IcT n -5- Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639A001300140001-5 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 gross extrusion of the seal had been encountered when the flange screws were tightened in an effort to insure a leak-tight joint. A threaded extension was provided on the end cap to permit attach- ment of the timer to a neutral-buoyancy chaiiber, which could be added later; a plug was incorporated in the threaded extension to facilitate the filling of the unit with the silicone fluid. A threaded extension was also added at the firing-pin end of the timer to permit attachment of the unit to the "workpiece". For experimental purposes, a piston-rod extension was arranged so that movement of the piston could be measured with a dial indicator in contact with the end of the piston-rod extension. Selection of Tiler i~ etering Tubes Light metering tubes, each 0.075 inch in OD x 0.010 inch in ID x 2 inches in length, were cut from a common piece of Type 321 stainless steel seamless capillary tubing. The tubes were debarred, inspected, and placed on a manifold for flow measurements. Each tube was inserted in a manifold adapter and held by two 0-rings; thus, the actual _etering-tube seal instal- lation was s4.; `ulated. Silicone fluid (Viscasil 500, 000) was extruded through these tubes for 21 days under a pressure of 70 psi and at an average a:cbient temperature of 77.5 F. The quantity of fluid extruded during each 24-hour period was collected in a covered container and weighed. The metering tubes and the manifold with related equipment are shown in Figure 2. Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Mrs Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 The total flow for each of seven of these metering tubes over a 21-day period varied from about 5.O) to 5.93 grams. A restriction in the eighth tube resulted in only 2.1.) ;rams of fluid being extruded during the sa: le period. Four metering tubes were then selected for assembly in the e:,peri:n-ental tti::.e-delay units. The tubes chosen were those which had extruded the ,ost sir filar. am mounts of fluid, namr,ely, 5.315, 5.313`% 5.533, ancd !Jra: s. .,also, based on these data, a spring was designed that would perm:-it the timer units to provide for the desired delay period of one year at an average temperature of 75 F. Fabrication and Asse_,-bly of the Tiriers The housing, end cap, cap at the firin pin end of the unit, aid :,:iscellaneous external parts were prepared from, cast 356 alu:inu: alloy hest treated to the T_ condition; this material was used because of its ;_;ood resistance to sea-water corrosion. The piston and Bellofrar washer were fabricated fro- 2024-Ty alur.inun alloy, and the piston-rod extension and dowel pins, fro:mr: drill rod. All of the parts and fluid passages were cleaned and inspected before final assembly. Individual parts and sub- assemblies of the experimental ti':1er (e, during which time they --;ere visually inspected; this procedure was used to insure that air bubbles trapped in the fluid could escape, through the filler-plug opening. when the air bubbles in the fluid had di ssioated, the filler plug was installed, and the meterini tube valve was :roved to the open position. The piston and sprint; subasser:bly was then installed; the fluid which consequently became surplus was allowed to flow through the metering tube until the "_:cyihole" in the piston moved sufficiently to line up with the _Deterin;- tube valve; and the valve was closed. Under a constant-temperature condition and with the valve closed, no further movement of the piston was expected unless a leakage of fluid occurred. The experimental units were subsequently installed in a previously converted refrigerator, which was adjusted to maintain a temperature of For several days the units in a non-operating condition were observed and no leakage of silicone fluid was noted. '_"his e,~-oer-i:rental time-delay unit had been designed so that the silicone fluid would be forced through the metering tube by the sprint; actin;, on the piston_, which was in contact with the Bellofram. piston seal; therefore, by means of measurements of the rate of piston travel, the amount of fluid disrlaced per unit of -time and, consequently, the t .':e-delay characteristics of the unit could be evaluated. In the laboratory set up used, the piston travel was measured with dial Indicators. Tack e, _ueri- : rental imer a.nc a dial indicator were mounted on a test stand with the Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 -12- ste:", of the dial indicator in contact with the piston-rod extension of the t i .ler. This arr anf;e:r'ent is shown In Figure '+. Following temperature stabilization of the experimental timers -n the constant-te::rerature boa (at about 75 F), the ?etering-tube valve was moved to the open position on each unit, and. the timers were actuated for operation at about 75 F. Results of Evaluation at 75 F. The flow characteristics of the four exreri -,.rental timers, as observed during the 5-month evaluation period, are illustrated in Figure 5. After the first 2 months of operation, three of the experimental ti.:-" timers (Taos. 1, `;, and ';) were within the tolerances of piston travel based on an allowable variation of 1-1/2 months per year. The values for total travel for the three units were 3,371.. 0. 382, and 0. 01 inch. he fourth Lm-it (:To. 0) showed a reduced flow almost from the start: this indicated sore restriction in the metering tube. During the third ?_onth, Ti? :,Ter No. 1 u:'denl?T show-e;~ a red=uced flow and then stoppa e. in the fourth month of operation, we_..ent of Timer i o. i; slo7ve,i dm,rn as a result of restricted flxv. In the eantime, Timer 1"o. 3 continued to operate with a slowly decreasing flow rate; at the end of 5 r..:onths, the amount of piston travel :a just outside the allowable variation based on the calculated. travel for 5 months . After two of the experimental timers showed an appreciable reduction in flo,.T rate, an investigation was made to locate the cause of the difficulty. During this investigation, an examination of the Viso as'_1 received from the manufacturer for use on this program Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 Sanitized Copy Approved for Release 2011/09/20: CIA-RDP78-03639AO01300140001-5 t6 7C)9 Figure 4. Laboratory Set Up for Ieasurinf- Piston Travel in L